I can't seem to get my motors to move.
I am using the mks tmc2209 v1 that came with the sgen L.
I removed the diag jumpers that were installed for sensorless homing since I read that the mks v1 2209 doesn't support it.
When I try to home any axis no motors move and the board halts with a "homing failed" message.
Any ideas? Here is the output from M122.
13:15:49.358 : X Y Z Z2 E
13:15:49.358 : Address 0 0 0 0 0
13:15:49.389 : Enabled false false false false false
13:15:49.389 : Set current 800 800 800 800 800
13:15:49.436 : RMS current 795 795 795 795 795
13:15:49.483 : MAX current 1121 1121 1121 1121 1121
13:15:49.483 : Run current 25/31 25/31 25/31 25/31 25/31
13:15:49.483 : Hold current 17/31 17/31 17/31 17/31 17/31
13:15:49.529 : CS actual 17/31 17/31 17/31 17/31 17/31
13:15:49.578 : PWM scale 20 20 20 20 20
13:15:49.625 : vsense 1=.18 1=.18 1=.18 1=.18 1=.18
13:15:49.656 : stealthChop true true true true true
13:15:49.703 : msteps 16 16 16 16 16
13:15:49.750 : tstep max max max max max
13:15:49.750 : pwm
13:15:49.750 : threshold 79 79 641 641 263
13:15:49.796 : [mm/s] 100 100 3 3 30
13:15:49.843 : OT prewarn false false false false false
13:15:49.890 : off time 0 0 0 0 0
13:15:49.937 : blank time 24 24 24 24 24
13:15:49.937 : hysteresis
13:15:49.984 : -end -1 -1 -1 -1 -1
13:15:50.015 : -start 1 1 1 1 1
13:15:50.015 : Stallguard thrs 0 0 0 0 0
13:15:50.015 : DRVSTATUS X Y Z Z2 E
13:15:50.062 : stst * * * * *
13:15:50.109 : olb
13:15:50.156 : ola
13:15:50.203 : s2gb
13:15:50.250 : s2ga
13:15:50.281 : otpw
13:15:50.328 : ot
13:15:50.375 : 157C
13:15:50.421 : 150C
13:15:50.468 : 143C
13:15:50.515 : 120C
13:15:50.515 : s2vsa
13:15:50.515 : s2vsb
13:15:50.515 : Driver registers:
13:15:50.515 : X 0xC0:11:00:00
13:15:50.531 : Y 0xC0:11:00:00
13:15:50.531 : Z 0xC0:11:00:00
13:15:50.546 : Z2 0xC0:11:00:00
13:15:50.562 : E 0xC0:11:00:00
13:15:50.562 : Testing X connection... OK
13:15:50.578 : Testing Y connection... OK
13:15:50.578 : Testing Z connection... OK
13:15:50.593 : Testing Z2 connection... OK
13:15:50.593 : Testing E connection... OK
I am using the mks tmc2209 v1 that came with the sgen L.
I removed the diag jumpers that were installed for sensorless homing since I read that the mks v1 2209 doesn't support it.
When I try to home any axis no motors move and the board halts with a "homing failed" message.
Any ideas? Here is the output from M122.
13:15:49.358 : X Y Z Z2 E
13:15:49.358 : Address 0 0 0 0 0
13:15:49.389 : Enabled false false false false false
13:15:49.389 : Set current 800 800 800 800 800
13:15:49.436 : RMS current 795 795 795 795 795
13:15:49.483 : MAX current 1121 1121 1121 1121 1121
13:15:49.483 : Run current 25/31 25/31 25/31 25/31 25/31
13:15:49.483 : Hold current 17/31 17/31 17/31 17/31 17/31
13:15:49.529 : CS actual 17/31 17/31 17/31 17/31 17/31
13:15:49.578 : PWM scale 20 20 20 20 20
13:15:49.625 : vsense 1=.18 1=.18 1=.18 1=.18 1=.18
13:15:49.656 : stealthChop true true true true true
13:15:49.703 : msteps 16 16 16 16 16
13:15:49.750 : tstep max max max max max
13:15:49.750 : pwm
13:15:49.750 : threshold 79 79 641 641 263
13:15:49.796 : [mm/s] 100 100 3 3 30
13:15:49.843 : OT prewarn false false false false false
13:15:49.890 : off time 0 0 0 0 0
13:15:49.937 : blank time 24 24 24 24 24
13:15:49.937 : hysteresis
13:15:49.984 : -end -1 -1 -1 -1 -1
13:15:50.015 : -start 1 1 1 1 1
13:15:50.015 : Stallguard thrs 0 0 0 0 0
13:15:50.015 : DRVSTATUS X Y Z Z2 E
13:15:50.062 : stst * * * * *
13:15:50.109 : olb
13:15:50.156 : ola
13:15:50.203 : s2gb
13:15:50.250 : s2ga
13:15:50.281 : otpw
13:15:50.328 : ot
13:15:50.375 : 157C
13:15:50.421 : 150C
13:15:50.468 : 143C
13:15:50.515 : 120C
13:15:50.515 : s2vsa
13:15:50.515 : s2vsb
13:15:50.515 : Driver registers:
13:15:50.515 : X 0xC0:11:00:00
13:15:50.531 : Y 0xC0:11:00:00
13:15:50.531 : Z 0xC0:11:00:00
13:15:50.546 : Z2 0xC0:11:00:00
13:15:50.562 : E 0xC0:11:00:00
13:15:50.562 : Testing X connection... OK
13:15:50.578 : Testing Y connection... OK
13:15:50.578 : Testing Z connection... OK
13:15:50.593 : Testing Z2 connection... OK
13:15:50.593 : Testing E connection... OK